Page created on 07/02/2025.
I’d like to make it clear from the outset that I have no illusions about the quality of such a tool, which costs less than €250, whereas a lathe considered to be more or less serious — I’m thinking of the Vevor or Proxxon models — starts at around €800.
My needs and my constraints don’t allow me these options: the most important constraint is the lack of space, which implies light equipment that’s easy to move around. Secondly, I’ll only be turning parts that are less than 50 mm, decorative and non-mechanical, requiring only relative accuracy.
The model chosen is from The First Tool. It is available from a number of sellers on AliExpress, with prices (pay attention to the power of the motor) and delivery times that vary quite a lot, depending on where it comes from — direct from China or a European country. Mine arrived from Germany in five days, even though the country advertised was Spain.
Website photo.
Inside the delivery box, the mini-lathe is held in a pre-formed cardboard shell. There’s nothing to assemble. As well as the machine itself, the packaging includes:
Website photo.
Finally, we discover a manual consisting of three A4 sheets, in English.
The design is based on extruded aluminium modules with dovetail grooves, measuring (w × h) 50 × 50 mm: a base, riser blocks, a motor block, a block for the feed and one for the tailstock. There is also, of course, a tool post.
The whole unit weighs 4.4 kg.
The blocks are fixed one on top of the other using double dovetail wedges with angled faces. The drawback of this system, as we’ll see, is that it doesn't allow the blocks to be clamped really parallel to each other. For this, it would have been necessary to have a parallel external clamping system, similar to the gibs on mobile carriages.
Click on the image for a closer look.
Transmission between the motor (12 V, 60 W) and the chuck shaft is via a toothed belt, protected by a plastic cover.
The spindle shaft is hollow, allowing cylindrical bars with a maximum diameter of 6.5 mm to pass through.
There is no drill chuck for the tailstock. The chuck and tailstock center are attached to their respective shafts by M12 × 1 threads.
Click on the image for a closer look at the spindles.
The tool post is supplied with a basic 4 mm square cutting tool. The other side of the tool post accepts a cross-section of up to 8 mm, but then the cutting edge will be too high in relation to the axis of rotation.
For your information, here are the dimensions of the tool post (cross-section).
The first thing to do is tighten all the screws, then adjust the clearance on the carriage slides. There are three: one for the feed, two for the tool post (cross-slide). Why two? Between the two is a graduated ring that allows the tool post to pivot. To adjust this, you have to loosen three pointed screws set at 120°, which are difficult to access. What’s more, their points mark the material and it becomes impossible to correct the default setting, as the screws return to their previous marks. I replaced them with standard M4 flat-head screws.
The slide clearance is also adjusted using point screws on plastic gibs. Here again, the tips of the screws dig into the gibs more and more as they are used, causing the play to reappear and even risking tearing the gibs sooner or later. These screws cannot be replaced by flat-ended screws, as they bear on a surface inclined at 60°: there would be a risk of the gib shifting under the thrust. These gibs, which are too soft, must therefore be replaced.
Ideally, I’d use 3 or even 3.5 mm aluminium sheet, but I only have 2 mm. So I doubled it with 1 mm polystyrene (PS) to act as an anti-friction layer.
I cut 9 mm wide strips of aluminium. I use the carriage body to hold them at a 60° angle so that I can mill their edges. I first place a 1 mm thick, 28 mm wide PS spacer at the bottom of the female dovetail, to raise the future gib a little and avoid the risk of machining the support itself.
Next, the gib is placed and secured with roughly shaped hardboard wedges, which are forced in. Check that the gib rests firmly on the PS spacer at the bottom of the dovetail.
The height of the ⌀ 6 milling cutter is set to remove 1 mm of material. After milling, deburring is carried out on the sharp edge. The gib is then turned over to machine the opposite edge.
To improve the adhesion of the glue, the surface opposite the adjustment screws is scratched with abrasive paper, along with the PS shim, then these two parts are glued together with C.A. glue. This will be enough to prevent them from moving against each other.
The old gib is on the right.
An initial adjustment is made without the feed screw: this gives a better feel for the friction. After assembling the slides, I tighten the pointed screws quite a bit to mark the gib and prevent it from moving. I then loosen the screws and tighten them again, sliding the moving part to feel the friction. It’s important that the gib returns to the same position after disassembly; to do this, I draw a mark with a felt-tip pen between the body and the gib.
The handwheels are mounted on their cylindrical shafts with a simple flat to prevent mutual rotation, and secured with a ‘Nylstop’ nut.
There is a space of 0.2 to 0.3 mm between the flats, giving a very large amount of play. To eliminate this, I make nickel silver shims measuring 15 x 2.5 x 0.2 or 0.3 mm (depending on the case). Each shim is scratched with sandpaper, as is the handwheel flat.
The shim is glued to the flat surface using CA glue. The edges of the shim are rounded with a file.
After reinstalling the feed screw with its washers in its bearing (and lubricating it), the handwheel head is reassembled and forced in.
Before reassembling, the screw is oiled and the slide bearings are greased with petrolatum.
The result is much smoother operation than before.
The chuck supplied has three zinc alloy jaws. Outside diameter: 48 mm. Minimum internal tightening: 2.5 mm; maximum tightening: approx. 25 mm.
Tightening the chuck is counter-intuitive, as you have to unscrew it to tighten it. It is locked not with a spanner, but with two pins supplied, one in the knurled part, the other in the jaw support.
Measuring concentricity with a dial gauge reveals an out-of-roundness of 16/100 mm.
Click on the image to see the other dial gauge position.
This out-of-roundness can only be corrected by machining the jaws with a drill in the tailstock, correctly aligned, which is not possible at the moment.
Alignment is checked between the tip of a centring pin and the travelling lathe center of the tailstock.
Click on the image for a closer look at the tips.
This offset exists in both the horizontal and vertical planes.
To compensate for the vertical offset, I placed two pieces of 0.1 mm copper strip under the lathe base block ①. For the horizontal offset, I placed two 0.2 mm pieces of nickel silver spacer between the same block and the vertical reinforcement plate ②..
Click on the image for a closer look at the spacers.
Warning: when I tighten the double dovetail inter-block fixings, the blocks can move and so lose the adjustment so painstakingly achieved. Clearly, this machine is not very well designed…
As already mentioned, the power cable entry is on the front, which is annoying. So I mill an identical cable entry at the rear of the motor block cover plate, mill ⌀ 6, depth 2 mm.
As also previously mentioned, there is no speed variation. I therefore fit a cable to connect the lathe to my laboratory power supply. It is fitted with a male ⌀ 5.5 × 2 power jack on the motor end; on the other end, with a male pin connecting block, which is my personal “standard” for very low voltage power supplies, both DC and DCC.
A drill chuck for mounting on the tailstock would be very useful, but is not supplied. It is fitted with an M12 × 1 thread.
Good to know: a a chuck with 4 independent jaws with the appropriate thread is available on AliExpress, but I have no use for it at the moment.
After a lot of searching (the M12 × 1 attachment is not common), I finally found a suitable drill chuck in the Unimat range. Unfortunately, this chuck doesn’t align properly with the spindle axis, probably because the thread clearance is too large.
Note: Chinese mini-lathes seem to be copies of the Unimat 1 Classic. The proof is in the pudding (but at almost twice the price!):
Photo on The Cool Tool.
From the same supplier, you can find precision brass collets and their fixing nut. And that is much better, except that… the diameter of the collet body (8.3 mm) is larger than the bore of the spindle (8−)!
I got away with re-boring the spindles using an 8.5 mm drill bit worn enough to come close to 8.3 mm, but I admit it’s not very rational!
The 4 mm square bar supplied was insufficient, so I bought a set of Proxxon tools. They fit into the tool post with a 0.7 mm shim to obtain the required height.
The concentricity of the chuck is restored using a drill collet on the tailstock side. With the chuck clamped as tight as possible, the first pass was made with a ⌀ 2.5 mm bit, the second at ⌀ 3 mm. Each jaw then had to be reworked for deburring. I finally achieved acceptable, though not perfect, concentricity.
I carried out tests with a round brass bar ⌀ 4 mm, using the Proxxon form 1 tool (cutting edge to the left, for turning). To obtain an acceptable surface finish, you need to rotate at high speed, with passes of no more than 0.1 mm and a slow feed rate. Despite these precautions, the part being machined can sometimes climb onto the tool and get stuck! The result: a damaged part that has to be remade!
Turning over about 12 mm with a 4/100 “finishing” pass, which was supposed to produce a cylinder with a diameter of 2 mm, resulted in a variation of 0.1 mm from one end to the other!
I also tried to drill a centre to use the tailstock, using a carbide ⌀ 1.5 mm drill — I don’t have a centring drill —, but this drill was off centre again, despite the care I had taken with the alignment setting.
After reading the above, you can imagine that I’m not delighted with my purchase.
As I said at the outset, I wasn’t expecting excellent results, but I was disappointed nonetheless! So I won’t recommend this machine under any circumstances, despite its flattering appearance. In fact, its modular design is its main flaw, resulting in a lack of rigidity, and misalignment.
Without really believing it, because I had exceeded the 15-day return period (if I understood correctly), I made a request for a refund, which was accepted within three days (the amount includes the item and shipping costs). A return label was sent to me. Well, the refund was made after two weeks.
For a similar footprint and weight, but at twice the price, Proxxon offers the FD 150/E “precision” lathe. I’m not sure that the quality is proportional to the price, but this mini-lathe offers some interesting features, such as quick release of the tailstock via a lever, two mechanical speeds, speed variation, etc. In addition, it accepts tapered shanks, and ER 11 collets.
See the promotional video on Youtube.
60W ref. TZ20002MR mini-lathe
Approx. €250 on AliExpress.
Four-jaw chuck
Ref. Z011A M12x1mm
€18,84 on AliExpress.
Chuck ref. 162090
Capacity ⌀ 0,6 to 6 mm
€19,90 at The Cool Tool.
Brass precision collets
Ref. 162460xx
€5,50 each at The Cool Tool.
Fixing nut
Ref. A1A000073
€8 at The Cool Tool.
Set of 6 cutting tools
Proxxon ref. 24524
Approx. €60 € at Contorion.
FD 150/E precision lathe
Proxxon ref. 24150
Approx. €500 at Contorion.